by Keith Dykes and
Ron Graham
Here is a synopsis of the above incident provided to me in a
Process Hazards Review training course: 12/02/84 Bhopal, India.
Methyl isocyanate release. 2,000+ deaths. Water entered a
methyl isocyanate (MIC) storage tank causing a runaway reaction
resulting in 2,000+ deaths, the worst industrial accident in
history.
[Dykes] Causal Factors:
- Three protective systems out of service.
The refrigeration system was taken out of service because
of operating costs and the high temperature alarm, indicating
an exothermic reaction was occurring, was reset high. The
scrubber was inadequately sized for a large release and was
under repair during the incident. The flare stack was out
of commission while part of the inlet line had been removed
for repair.
- Plant was understaffed due to costs.
- Very high inventory of MIC, an extremely toxic
material.
- The accident occurred in the early morning.
- Most of the people killed lived in a shanty town
located very close to the plant fence.
[Graham] Union Carbide has produced a 17-minute
video on their failure investigation, entitled "Unraveling the
Tragedy at Bhopal." (This video I happened to stumble across
in the public library.) Here are a few notes:
The plant at Bhopal was used to manufacture pesticides, and a
primary chemical component of these pesticides is MIC. This
material reacts violently with water, and this reaction is what
caused the gaseous release. In this case, some 2500 lbf of water
got into the MIC storage tank, suggesting that a simple leak was
extremely unlikely. It was eventually reported by UCC that a
disgruntled employee, apparently working alone, removed a
pressure gauge directly attached to the tank, and just stuck
in a hose and filled the tank with water. (Many researchers,
however, doubt this claim, and UCC doesn't help its validity
by identifying any characteristics of the saboteur.) This
happened while plant supervisors were on break. There was
no valve failure involved at first.
Workers made the following attempts to save the plant:
- They tried to turn on the plant refrigeration system
to cool down the environment and slow the reaction.
(The refrigeration system had been drained of coolant
weeks before and never refilled -- it cost too much.)
- They tried to route expanding gases to a neighboring
tank. (The tank's pressure gauge was broken and
indicated the tank was full when it was really empty.)
- They tried to purge the gases through a scrubber.
(The scrubber was designed for flow rates, temperatures
and pressures that were a fraction of what was by this
time escaping from the tank. The scrubber was as a
result ineffective.)
- They tried to route the gases through a flare tower
-- to burn them away. (The supply line to the flare
tower was broken and hadn't been replaced.)
- They tried to spray water on the gases and have them
settle to the ground -- by this time the chemical
reaction was nearly completed. (The gases were
escaping at a point 100 feet above ground; the hoses
were designed to shoot water up to 40 feet in the air.)
Failing all those attempts, most fled for their lives.
When Union Carbide sent in a team to start the failure
investigation, the team was stonewalled by the Indian government,
which seized records and denied the team access to the plant, the
records and the eyewitnesses. A year or so later, the blackout
was lifted (via a USA court order), and the team found that
workers had changed or deleted records, eyewitnesses had left the
area to find new jobs and were difficult to track down, and some
witnesses who were found quickly had contradictory stories to
tell.
There are two sets of lessons learned here: those Union Carbide
did tell, and those they did not. Here's what they did tell us:
- When eyewitness interviews are required to determine the root
causes of failures, those interviews need to be conducted as
quickly as possible after the failure. The probability of
losing key witnesses or of getting contradictory information
back increases with time.
There were other things they mentioned, but this was the one
most significant point. They knew the engineering
cause of the failure early in the investigation.
What they didn't know was whodunit. Here's what they
didn't tell us:
-
There was no redundancy involved in physically checking the
storage tanks, and with the supervisors on break a golden
opportunity arose for a disgruntled employee to do mischief
undetected -- indeed, he was the tank-checker.
He knew his way around; he knew what water would do in the tank
(although he could not have known how much);
and he had a motive. Engineers cannot be expected to be
detectives (at least, not before the fact), but they certainly
can have back-ups -- two plant workers checking each structure
along independent paths. That would have prevented such an
enormous quantity of water from being introduced.
- As far as I could tell from review of the failure
investigation, there was no alarm system in the plant
sufficient to warn the nearby public. In a
case such as this, with harmful chemicals stored so close to
a densely-populated neighborhood, there probably should not
only have been a public alarm system, but possibly plant
first-aid personnel available to the locals.
- If you know that MIC reacts violently with water, then why
in Heaven's name would a water source be located so close
to a storage tank that water could be fed to the tank with
a hose? The water source needed to be somewhere else, or
inaccessible except in emergencies. Even fires around the
tank could be put out by other means. The MIC could perhaps
have been stored in several smaller tanks, limiting the
damage caused by one; there could perhaps have been a
pressure-activated bleed valve into an empty holding tank
for vapors.
- An emergency evacuation plan may have been in place, and
may even have been drilled by plant employees. But such
an evacuation plan should include the locals as well, and
if it wasn't in place, there was another problem.
- Finally, I was unable to tell whether the leak could have
been contained. Based on what Union Carbide presented, I
cannot but assume that the storage tanks were not even
in a building.
The failure investigation team of course cannot be held
accountable for not presenting this stuff in
their video, because it's likely to cast Union Carbide in
somewhat of a bad light -- and one of the purposes of the
video was to show the rigor of the failure investigation
under some really bad circumstances. Nevertheless, you can
bet that UC learned some valuable lessons about containment,
redundancy, buffer zones and alarms as a result of this
terrible accident.
Subsequent articles published by the Village Voice
and others indicate the following aftermath: